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Probably the scariest well I've been on in the GOM DW was about 6 years ago. They had set csg and were drilling ahead at 22,000'. And then they started to loss circ. They weren't sure where but it might have been at the previous csg shoe. They lost 60,000 bbls of OBM while drilling. No mud ever returned to the surface. So no mud log telling them if they had drilled oil/NG, no LWD to estimate pore pressure, no mud parameters to tell if the MW was being cut by oil, NG or water. And most importantly, no way to tell if the well was kicking. They put very heavy drill mud on the outside of the drill pipe but that would have not stopped a blow out coming up the inside of the DP. Took me 6 days to log that 2,500' of open hole. I ran pressure logs in the wet reservoir they cut: 19,000 psi bottom hole pressure. They were probably very lucky they didn't find oil/NG in that sand: a blow out could have easily happened. How scary was it? Some of the hands were sleeping in the escape capsules when they were off tower. And this insane risk was taken by a well known and very experience operator. Needless to say someone very high up in the company was willing to risk the 130 souls onboard that drillship to get this well down. Equally needless to point out: that person never set foot on that rig. We just finished the job, went home, cashed our pay checks and then tried to forget about it.

http://europe.theoildrum.com/node/6526#more

by asdf on Sun Jun 6th, 2010 at 06:41:05 PM EST
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